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May 2013 · Energy-Tech Magazine
February 2012 Go to Page 1 2
Apps are nice, but brainpower is better

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In his gentle way Double G asked Jimmy if he could handle the controls, and after a few minutes he determined that the IT folks had set the compression ratios to about 10 percent in order to conserve disk space. At a 10 percent compression ratio, the only thing you could monitor was if the plant had tripped or not. We told Jimmy that we would kick in a 1 terabyte disk that would hold about 10 years of plant data and he could have his IT department reset the compression ratios to about 0.1 percent.  

After going to another computer where more data was available, we started looking in earnest. The first thing we noticed was there was very little temperature rise across the second point feedwater heater. Normally this heater should have about a 50°F temperature rise but it now had about 13°F.

I wrote that down in my little black book and we continued our search. The heater pressure was also low and Jimmy said that the pressure indicator was not working. After a few hours of data review, we thought it was time to put our new knowledge from the safety video to use and do a plant walk down.

During this walk down we walked over to the heater in question and noticed that the extraction supply to the heater indicated “Open” (this is why they said that the pressure indicator was not working). Double G pointed out that it is odd that the temperature and the pressure indicator would fail at the same time. From the plant data we also noted that the temperature rise to the downstream heater was very high. Now our curiosity was piqued; I asked Double G to break out the computer model. It was time to test a hypothesis.

Here are the facts that we uncovered:

  • Temperature rise across the heater was low
  • Pressure of the heater shell was low
  • Heater Drain Valve was indicating almost closed
  • Heater Extraction Supply Valve was indicating open
  • Heater emergency dump valve was indicating closed and the downstream temperature was low
  • Computer model simulations indicate that the plant data is consistent with the heater being out of service
  • Temperature rise across downstream heater was high


It was clear that any problem – except a lack of steam getting to the heater – would have to have multiple failures, so referring to “Occam’s razor” we decided to suggest the simplest answer. The Steam Valve was actually closed when it indicated open.

Using a model we developed for the plant, Double G simulated a heater with the steam supply valve closed, and everything lined up like the real plant.

Data was collected before and after the outage where the anomaly occurred. A set of data at a common load and backpressure was chosen to represent operation before and after the event. The model had a set main steam flow that was representative of the plants general operating load. Plant data was selected based on similar condenser pressures to remove any variation related to the low pressure turbine last stage efficiency. Only the main steam flow, back pressure and affected feedwater heater tube side outlet temperatures were set. All other parameters were dynamic in the model. The heat rate calculated by the computer model is based on gross power, but does not include boiler efficiency effects. For this comparative study there were no sprays or boiler blow down.

One would think that management would have been happy not to tear apart their turbine, but they gave Jimmy a hard time about it. Fortunately Jimmy stuck to his guns and reminded them that this was a recommendation from someone more than 50 miles away who owned (and sometimes wears) a tie. As it turns out, the next outage they looked at the valve and the stem had separated from the disc.

The lesson from this story: Jimmy had all the tools one could ask for but they could not do the job for him. My iPhone apps are a great thing, but as I just learned while using the level app, you have to keep your brain engaged and not let the software make your logic fuzzy (pun intended). You may be thinking that we did use an app (the computer model) but that was used after the brain, it’s always the order of things that’s important. You also might be wondering about the PRB change.

You’re right, there was an issue, but that’s for another article …


Mr. Megawatt is Frank Todd, manager of Thermal Performance for True North Consulting. True North serves the power industry in the areas of testing, training and plant analysis. Todd’s career, spanning more than 30 years in the power generation industry, has been centered on optimization, efficiency and overall Thermal Performance of power generation facilities. He can be contacted at editorial@woodwardbizmedia.com.
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